TWA Flight 841 (1979): Difference between revisions
Newtonator (talk | contribs) ALPA concluded a lower rudder hardover was what really caused the upset and the NTSB developed a biased notion on what they feel caused the upset. |
TG-article (talk | contribs) Changing short description from "1979 aviation accident" to "Aviation accident in Michigan, U.S." |
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{{Short description| |
{{Short description|Aviation accident in Michigan, U.S.}} |
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{{For|the 1974 |
{{For|the 1974 bombing with the same flight number|TWA Flight 841 (1974)}} |
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{{Use mdy dates|date=January 2016}} |
{{Use mdy dates|date=January 2016}} |
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{{Infobox aircraft occurrence |
{{Infobox aircraft occurrence |
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|name=TWA Flight 841 |
| name = TWA Flight 841 |
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|image |
| image = Trans World Airlines - TWA Boeing 727-31 N840TW (No Watermark).jpg |
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| image_upright = 1.15 |
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|image_size = 250px |
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|alt = |
| alt = |
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|caption |
| caption = N840TW, the aircraft involved, four years before the accident |
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|date=April 4, 1979 |
| date = April 4, 1979 |
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|type=Uncontrolled descent |
| type = Uncontrolled descent; cause disputed |
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| occurrence_type = Accident |
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Cause disputed: |
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| site = Over [[Saginaw, Michigan]], United States |
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| aircraft_type = [[Boeing 727|Boeing 727-31]] |
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• Leading edge slat failure ([[National Transportation Safety Board|NTSB]]) |
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| operator = [[Trans World Airlines]] |
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• Yaw damper induced lower rudder hardover ([[Air_Line_Pilots_Association,_International|ALPA]]) |
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| IATA = TW841 |
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|occurrence_type=Accident |
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| ICAO = TWA841 |
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|site= Over [[Saginaw, Michigan|Saginaw]], [[Michigan]], [[United States]] |
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| callsign = TWA 841 |
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|aircraft_type=[[Boeing 727|Boeing 727-31]] |
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| origin = [[John F. Kennedy International Airport]],<br>[[New York City]], U.S. |
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|operator=[[Trans World Airlines]] |
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| destination = [[Minneapolis-Saint Paul International Airport]],<br>[[Minneapolis, Minnesota|Minneapolis]], U.S. |
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|callsign=TWA 841 |
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| tail_number = N840TW |
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|origin=[[John F. Kennedy International Airport]],<br>[[New York City]], U.S. |
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| occupants = 89 |
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|destination=[[Minneapolis-Saint Paul International Airport]],<br>[[Minneapolis, Minnesota|Minneapolis]], U.S. |
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| fatalities = 0 |
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|tail_number=N840TW |
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| injuries = 8 |
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|occupants=89 |
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| passengers = 82 |
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|fatalities=0 |
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| crew = 7 |
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|Injuries=8 |
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| survivors = 89 |
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|passengers=82 |
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|crew=7 |
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|survivors=89 |
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}} |
}} |
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'''TWA Flight 841''' was a scheduled passenger flight from [[John F. Kennedy International Airport]] |
'''TWA Flight 841''' was a scheduled passenger flight from [[John F. Kennedy International Airport]], New York City, en route to [[Minneapolis-Saint Paul International Airport]] in Minneapolis, Minnesota. On the evening of April 4, 1979 while flying over [[Saginaw, Michigan|Saginaw]], [[Michigan]], the [[Boeing 727|Boeing 727-31]] airliner began a sharp, uncommanded [[Flight dynamics|roll]] to the right, and subsequently went into a [[spiral dive]]. The pilots were able to regain control of the aircraft and made an emergency landing at [[Detroit Metropolitan Airport]]. |
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== |
== Background == |
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At 8:25{{nbs}}p.m. [[Eastern Time Zone|EST]], TWA Flight 841 departed JFK International after a 45-minute delay due to traffic congestion and reached its initial cruising altitude of 35,000{{nbs}}feet at 8:54{{nbs}}p.m. Due to a {{nowrap|100-knot}} headwind, the pilots requested to climb to 39,000{{nbs}}feet at 9:25{{nbs}}p.m., which was granted. At 9:49{{nbs}}p.m., after traveling nearly {{convert|540|miles|km}},<ref>{{cite web|url=http://www.distancefromto.net/|title=Distance Between Cities Places On Map Distance Calculator|publisher=|accessdate=February 6, 2017}}</ref> while cruising at {{convert|39000|ft|m}} near the city of Saginaw, Michigan, Captain Harvey "Hoot" Gibson (44),<ref>{{cite web |last1=Corsetti |first1=Emilio |title=Hoot Gibson Remembered |url=https://emiliocorsetti.com/hoot-gibson-remembered/ |website=Scapegoat: A Flight Crew’s Journey from Heroes to Villains to Redemption |date=February 2015 |access-date=20 September 2022}}</ref> said the aircraft was operating with the [[autopilot]] on "Altitude Hold" mode when he felt a high frequency vibration in the balls of his feet, followed by a buzzing sound and a light buffeting of the airframe. He saw the plane's nose yaw to the right, pause and then yaw right again. He looked at his instruments and saw the plane banking right with the autopilot moving the control wheel to the left to level the wings. This had no effect so Gibson disconnected the autopilot and applied full left aileron which had no effect. He got on the rudder pedals to apply full left rudder. He would state that as he did so he felt something didn't feel right with the rudder but didn't know what it was. Captain Gibson's inputs had no effect as the plane very quickly began a steep roll to the right.<ref name="AAR-81-08 Final Report">{{cite book|date=June 9, 1981 |publisher=[[National Transportation Safety Board]]|url=https://www.ntsb.gov/investigations/AccidentReports/Reports/AAR8108.pdf|title=Aircraft Accident Report - Trans World Airlines, Inc., Boeing 727-31, N840TW, Near Saginaw, Michigan April 4, 1979}}</ref>{{rp|2}} Gibson shouted "Get em' up!" referring to the co-pilot to deploy the speed brakes, but the co-pilot didn't understand what the Captain meant so Gibson deployed them. Despite the best efforts of the flight crew, the aircraft spiraled out of control; Gibson shouted, "We're going over!". Flight 841 dived about {{convert|34000|ft|m}} in just 63{{nbs}}seconds.<ref name="AAR-81-08 Final Report" />{{rp|2}} During the course of the dive, the plane rolled through 360{{nbs}}degrees twice and exceeded the [[Mach number|Mach]] limit for the 727 [[airframe]]. During the dive, Captain Gibson got so desperate to save the plane that he began moving his control column from all the way left to all the way right, then all the way forward and all the way back, full left rudder, then full right rudder, and retracted and extended the speedbrakes, but his efforts were fruitless. |
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=== Aircraft === |
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At about {{convert|15000|ft|m}} the pilots extended the [[landing gear]] in an attempt to slow the aircraft. A few seconds after extending the gear, Captain Gibson managed to regain control and pull the 727 out of its dive, and at about {{convert|5000|ft|m}} the nose finally came up again.<ref name="Peterson, Iver 1979">Peterson, Iver. "Plane Passengers Prayed But Expected to Be Killed." [[The New York Times]] (April 7, 1979), 6.</ref><ref>''The Post-Standard'' (Syracuse, New York), June 10, 1981, page 11</ref> The plane suffered substantial structural damage with the System A hydraulics ruptured as a result of the right main landing gear overextending but made an emergency landing at [[Detroit Metropolitan Airport]] in Michigan at 10:31{{nbs}}p.m. [[Eastern Time Zone|EST]] without further trouble. No fatalities occurred among the 82{{nbs}}passengers and 7{{nbs}}crew members. Eight passengers reported minor injuries related to high {{nowrap|[[g-force]]s}}.<ref name="AAR-81-08 Final Report" /> |
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The aircraft involved, manufactured in 1965, was a 13 year old Boeing 727-31, [[Aircraft registration|registered]] as N840TW with [[serial number]] 18905. In its 14 years of service, it had accumulated about 35,412 hours.<ref name="AAR-81-08 Final Report" />{{Rp|page=8}} |
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=== Crew === |
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In command was [[Pilot in command|Captain]] Harvey G. "Hoot" Gibson, aged 44, who had logged a total of 15,710 piloting hours, 2,597 of them on the 727. The day before he had returned to flying following a three month medical leave.<ref name="AAR-81-08 Final Report" />{{rp|4}} The [[First officer (aviation)|First Officer]] was J. Scott Kennedy, aged 40, who had logged a total of 10,336 total piloting hours, 8,348 of them on the 727. The [[flight engineer]] was Gary N. Banks, 37, who had logged a total of 4,186 piloting hours, 1,186 of them on the 727.<ref name="AAR-81-08 Final Report" />{{rp|8}} |
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== Accident == |
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At 8:25{{nbs}}p.m. [[Eastern Time Zone|EST]], TWA Flight 841 departed JFK International after a 45-minute delay due to traffic congestion and reached its initial cruising altitude of 35,000{{nbs}}feet at 8:54{{nbs}}p.m. Due to a {{nowrap|100-knot}} headwind, the pilots requested to climb to 39,000{{nbs}}feet at 9:25{{nbs}}p.m., which was granted. At 9:47{{nbs}}p.m., while cruising at {{convert|39000|ft|m}} near the city of Saginaw, Michigan, Captain Gibson said the aircraft was operating with the [[autopilot]] on "Altitude Hold" mode when he felt a high frequency vibration in the balls of his feet, followed by a buzzing sound and a light buffeting of the airframe. He looked at his instruments and saw the plane banking right before yawing sharply to the right, briefly pausing, and yawing right again into a skidding right roll with the autopilot moving the control wheel to the left to level the wings.<ref name=Emergency!/>{{rp|page=194-195}} Gibson disconnected the autopilot and applied full left aileron which had no effect. He got on the rudder pedals and applied full left rudder. As he did so something didn't feel right but he couldn't place it.<ref name=Emilio/>{{rp|page=11}} Although Captain Gibson's inputs briefly stopped the roll from increasing, the roll continued and the aircraft spiraled out of control. Gibson shouted something to the effect of "We're going over!"<ref name="AAR-81-08 Final Report">{{cite book|date=June 9, 1981 |publisher=[[National Transportation Safety Board]]|url=https://www.ntsb.gov/investigations/AccidentReports/Reports/AAR8108.pdf|title=Aircraft Accident Report - Trans World Airlines, Inc., Boeing 727-31, N840TW, Near Saginaw, Michigan April 4, 1979}} - [https://libraryonline.erau.edu/online-full-text/ntsb/aircraft-accident-reports/AAR81-08.pdf Copy at] [[Embry-Riddle Aeronautical University]].</ref>{{rp|6}} After completing one 360° roll, Gibson shouted to the co-pilot "Get em' up!" referring him to deploy the [[speed brakes]], but the co-pilot didn't understand what the Captain meant so Gibson deployed them which also had no effect.<ref name="AAR-81-08 Final Report" />{{rp|2-3}} |
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Flight 841 dove about {{convert|34000|ft|m}} in just 63{{nbs}}seconds.<ref name="AAR-81-08 Final Report" />{{rp|2}} During the course of the dive, the plane rolled through 360{{nbs}}degrees at least twice and exceeded the [[Mach number|Mach]] limit for the 727 [[airframe]]. |
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At about {{convert|15000|ft|m}} the pilots extended the [[landing gear]] in an attempt to slow the aircraft. A few seconds after extending the gear, Gibson managed to regain control and pulled the 727 out of its dive at about {{convert|5000|ft|m}}.<ref name="Peterson, Iver 1979">Peterson, Iver. "Plane Passengers Prayed But Expected to Be Killed." [[The New York Times]] (April 7, 1979), 6.</ref><ref>''The Post-Standard'' (Syracuse, New York), June 10, 1981, page 11</ref> The plane suffered substantial structural damage with the No.7 [[leading-edge slat]] and a flight spoiler having detached, the right outboard aileron hinge fitting broke due to metal fatigue resulting in free-play, and the System A hydraulics ruptured due to the right main gear overextending which also broke the sidebrace and actuator support beam; the Flight Engineer reported they had a fail flag for the lower rudder [[yaw damper]]<ref name="AAR-81-08 Final Report" />{{rp|10}} but made an emergency landing at [[Detroit Metropolitan Airport]] in Michigan at 10:31{{nbs}}p.m. [[Eastern Time Zone|EST]] without further trouble. After landing and shutting the engines down the pilots turned on the [[Auxiliary Power Unit]] (APU) as a mechanic plugged into an intercom to talk to the pilots and reported fuel was leaking from the left side. All 89 people deplaned via the aft [[airstair]] with only eight passengers suffering minor injuries.<ref name="AAR-81-08 Final Report" /> |
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==Investigation== |
==Investigation== |
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Several days after the upset, the aircraft was sufficiently repaired to be ferried to Kansas City for further repairs instead of being preserved for tests and in-depth analysis of components and systems in order to conclusively determine what happened; it returned to service in May 1979.<ref name="AAR-81-08 Final Report" />{{rp|4}} The flight crew would be questioned on three occasions during the course of the entire investigation: hours after landing in Detroit, on April 12, 1979, and on January 29, 1980.<ref name="AAR-81-08 Final Report" />{{rp|37}} The investigators of the [[National Transportation Safety Board]] (NTSB) located the No. 7 [[Leading-edge slats|slat]] missing from the leading edge of the right wing amongst other parts that had detached. They requested that [[Boeing]], the manufacturer, inspect the remainder of the slat assembly, including a portion of the slat actuator cylinder (the motor that moves the slat and holds it in position). Boeing determined that the No. 7 slat had failed because the slats had been extended while the aircraft was flying at cruising speed. They also determined that it was "impossible" for the slat to extend without manipulating the controls.<ref name="auto">{{cite web|url=https://www.youtube.com/watch?v=JYHfrk6EVHU |archive-url=https://ghostarchive.org/varchive/youtube/20211215/JYHfrk6EVHU |archive-date=2021-12-15 |url-status=live|title=The Plane That Fell From The Sky (Full Version) TWA 841|last=otosflashymoon|date=September 17, 2012|publisher=|accessdate=February 6, 2017|via=YouTube}}{{cbignore}}</ref>{{Bsn|date=August 2024}} |
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The [[National Transportation Safety Board]] (NTSB) investigated the accident, conducting what was at the time the lengthiest accident investigation in NTSB history.<ref name="Tribune 1990.10.14">{{cite web|url=http://articles.chicagotribune.com/1990-10-14/news/9003260194_1_twa-flight-test-flight-flight-attendants|title=11 Years After Plane Took A Dive, Pilot Tries To Clear His Reputation|publisher=[[Chicago Tribune]]|date=October 14, 1990|accessdate=February 6, 2017}}</ref> In its final report, published in June 1981, the NTSB concluded the probable cause of the accident was a mechanical failure of a [[leading-edge slat]] under inappropriate manipulation and the captain's untimely action.<ref name="AAR-81-08 Final Report" />{{rp|1}} |
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The TWA Flight 841 investigation would be at the time the lengthiest accident investigation in the NTSB's history.<ref name="Tribune 1990.10.14">{{cite web|url=https://www.chicagotribune.com/1990/10/14/11-years-after-plane-took-a-dive-pilot-tries-to-clear-his-reputation/|title=11 Years After Plane Took A Dive, Pilot Tries To Clear His Reputation|publisher=[[Chicago Tribune]]|date=October 14, 1990|access-date=February 6, 2017}}</ref> After eliminating all known sources of mechanical failure, the NTSB concluded in June 1981 in its final report, that the probable cause of the accident was the isolated extension of the No. 7 [[leading-edge slat]] from the flight crew manipulating the flap/slat controls in an inappropriate manner leading to an uncommanded roll to the right and the captain's untimely action.<ref name="Witkin, Richard 1980">Witkin, Richard. "[https://www.nytimes.com/1980/01/18/archives/safety-board-hints-crew-errors-may-have-led-to-jet-dive-over.html Safety Board Hints Crew Errors May Have Led to Jet Dive Over Michigan]." [[The New York Times]] (January 18, 1980), A10.</ref><ref name="AAR-81-08 Final Report" />{{rp|1-2}} |
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Among the damage discovered after the accident, investigators found the #7 [[Leading-edge slats|slat]] missing from the leading edge of the right wing. NTSB investigators requested the aircraft manufacturer, [[Boeing]], inspect the remainder of the slat assembly, including a portion of the slat actuator cylinder (the motor that moves the slat and holds it in position). Boeing determined that the #7 slat had failed because the slats had been extended while the aircraft was flying at cruising speed. They also determined that it was "impossible" for the flaps to extend without manipulating the controls.<ref name="auto">{{cite web|url=https://www.youtube.com/watch?v=JYHfrk6EVHU |archive-url=https://ghostarchive.org/varchive/youtube/20211215/JYHfrk6EVHU |archive-date=2021-12-15 |url-status=live|title=The Plane That Fell From The Sky (Full Version) TWA 841|last=otosflashymoon|date=September 17, 2012|publisher=|accessdate=February 6, 2017|via=YouTube}}{{cbignore}}</ref> |
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{{Blockquote|text=The Safety Board determines that the probable cause of this accident was the isolation of the No. 7 leading-edge slat in the fully or partially extended position after an extension of the Nos. 2, 3, 6 and 7 leading-edge slats and the subsequent retraction of the Nos. 2, 3, and 6 slats, and the captain's untimely flight control inputs to counter the roll resulting from the slat asymmetry. Contributing to the cause was a preexisting misalignment of the No. 7 slat which, when combined with the cruise condition airloads, precluded retraction of that slat. After eliminating all probable individual or combined mechanical failures, or malfunctions which could lead to slat extension, the Safety Board determined that the extension of the slats was the result of the flightcrew's manipulation of the flap/slat controls. Contributing to the captain's untimely use of the flight controls was distraction due probably to his efforts to rectify the source of the control problem.<ref name="AAR-81-08 Final Report" />{{rp|1}}}} |
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After eliminating all individual and combined sources of mechanical failure, the NTSB ruled that the extension of the slats was due to the flight crew manipulating the flap/slat controls in an inappropriate manner.<ref name="AAR-81-08 Final Report" />{{rp|2}}<ref name="Witkin, Richard 1980">Witkin, Richard. "Safety Board Hints Crew Errors May Have Led to Jet Dive Over Michigan." [[The New York Times]] (January 18, 1980), A10.</ref> Investigators believed that 727 pilots (in general, and this flight specifically) were setting the trailing edge flaps to two degrees during high altitude cruise, while at the same time pulling the circuit breaker for the slats so that they would not activate. This configuration was rumored to result in increased lift with no increase in drag, thus allowing more speed, higher elevation, or decreased fuel consumption. Flaps and slats were intended to only be deployed at low speeds during take-off or landing.<ref name="AAR-81-08 Final Report" /> |
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Investigators believed that 727 pilots (in general, and this crew specifically) were enabling the trailing edge flaps to extend independently of the slats via the flap/slat lever by turning the Alternate flap switch on, pulling the leading-edge slats circuit breaker, turning the Alternate flap switch off and then setting the flaps to two degrees during high altitude cruise. This configuration was rumored to result in increased lift with no increase in drag, thus allowing more speed, higher elevation, or decreased fuel consumption. Flight tests showed that airspeed and performance decreased in this configuration. Flaps and slats are intended to only be deployed at low speeds during take-off and landing.<ref name="AAR-81-08 Final Report" /> |
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The crew, Capt. Harvey G. "Hoot" Gibson (1934-2015),<ref>{{cite web | url=https://emiliocorsetti.com/hoot-gibson-remembered/ | title=Hoot Gibson remembered| date=February 2015}}</ref> first officer J. Scott Kennedy (1939-2017),<ref>{{cite web | url=https://emiliocorsetti.com/the-passing-of-scott-kennedy/ | title=The passing of Scott Kennedy | date=October 26, 2017 }}</ref> and flight engineer Gary N. Banks (born 1942), denied that their actions had been the cause of the flaps' extension: {{Blockquote|text=At no time prior to the incident did I take any action within the cockpit either intentionally or inadvertently, that would have caused the extension of the leading edge slats or trailing edge flaps. Nor did I observe any other crew member take any action within the cockpit, either intentional or inadvertent, which would have caused the extension.|sign=Capt. Gibson<ref>Witkin, Richard. "Crew Will Testify Today On Near-Fatal Jet Plunge." [[The New York Times]] (Apr 12, 1979), B10.</ref><ref>Lindsey, Robert. "Pilot Says Extending Landing Gear Was Near Last Resort to Stop Dive." [[The New York Times]] (Apr 13, 1979), A16.</ref>}} |
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The crew, Capt. Harvey G. "Hoot" Gibson (1934–2015),<ref>{{cite web | url=https://emiliocorsetti.com/hoot-gibson-remembered/ | title=Hoot Gibson remembered| date=February 2015}}</ref> First Officer J. Scott Kennedy (1939–2017),<ref>{{cite web | url=https://emiliocorsetti.com/the-passing-of-scott-kennedy/ | title=The passing of Scott Kennedy | date=October 26, 2017 }}</ref> and Flight Engineer Gary N. Banks (born 1942), denied that their actions had been the cause of the flaps' extension: {{Blockquote|text=At no time prior to the incident did I take any action within the cockpit either intentionally or inadvertently, that would have caused the extension of the leading edge slats or trailing edge flaps. Nor did I observe any other crew member take any action within the cockpit, either intentional or inadvertent, which would have caused the extension.|sign=Capt. Gibson<ref>Witkin, Richard. "[https://www.nytimes.com/1979/04/12/archives/crew-will-testify-today-on-nearfatal-jet-plunge-3-passengers.html Crew Will Testify Today On Near-Fatal Jet Plunge]." [[The New York Times]] (Apr 12, 1979), B10.</ref><ref>Lindsey, Robert. "[https://www.nytimes.com/1979/04/13/archives/pilot-says-extending-landing-gear-was-near-last-resort-to-stop-dive.html Pilot Says Extending Landing Gear Was Near Last Resort to Stop Dive]." [[The New York Times]] (Apr 13, 1979), A16.</ref>}} |
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The crew suggested instead that an actuator on the #7 slat had failed, causing its inadvertent deployment. The NTSB rejected this as improbable and attributed the extension of the flaps to the deliberate actions of the crew. The crew claimed that such failures had happened on other 727s prior and subsequent to this incident.<ref>Boeing Operations Manual Bulletin, OMB 75-7, March 10, 1976; Subject: "Leading Edge Slat Actuator Lock Rings"; outlined specific conditions which had previously resulted in a Leading Edge Slat being pulled from the Retracted position (Mach > .8M, with failure of "A" System Hydraulic pressure to the slat actuator, with SpeedBrakes/Spoilers Extended).</ref> The NTSB report noted that between 1970 and 1973, seven separate cases involving a single leading edge slat extension and separation were reported, but none of these reports indicated whether or not the slat extension was due to flight crew involvement.<ref name="AAR-81-08 Final Report" />{{rp|18}} Records after 1974 did include this information, and (other than Flight 174) only two slat extension problems were reported between 1974 and the close of the NTSB's investigation in 1981, one of which was inadvertently caused by the flight crew.<ref name="AAR-81-08 Final Report" />{{rp|24}} However, in none of these previous cases did the plane become uncontrollable. |
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The flight crew testified that they had not engaged the flaps and instead suggested that the actuator to the No. 7 slat had failed, causing its inadvertent deployment. The NTSB concluded that "if the flight crew's recollections are accurate," the slat extension must have been caused by a mechanical failure or defect but ultimately rejected this as improbable and attributed the extension of the flaps to the deliberate actions of the crew.<ref name="AAR-81-08 Final Report" />{{rp|24}} The crew maintained that such failures had happened on other 727s prior and subsequent to this incident.<ref>Boeing Operations Manual Bulletin, OMB 75-7, March 10, 1976; Subject: "Leading Edge Slat Actuator Lock Rings"; outlined specific conditions which had previously resulted in a Leading Edge Slat being pulled from the Retracted position (Mach > .8M, with failure of "A" System Hydraulic pressure to the slat actuator, with SpeedBrakes/Spoilers Extended).</ref> The NTSB report noted seven separate cases involving a single leading edge slat extension and separation were reported between 1970 and 1973, but none of these reports indicated whether or not the slat extension was due to flight crew involvement.<ref name="AAR-81-08 Final Report" />{{rp|18}} Records after 1974 did include two report slat extensions between 1974 and towards the end of the NTSB's investigation in 1981, one of which was inadvertently caused by the flight crew. However, in none of these previous cases did the flights experience significant problems.<ref name="AAR-81-08 Final Report" />{{rp|24}} |
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The flight crew testified that they had not engaged the flaps, and the NTSB concluded that "if the flightcrew's recollections are accurate," the slat extension must have been caused by a mechanical failure or defect.<ref name="AAR-81-08 Final Report" />{{rp|24}} However, the NTSB ultimately concluded that the flight crew was probably attempting to use 2º of flaps at cruising speed: |
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{{Blockquote|text=While cruising at Mach 0.816 and 39,000 feet pressure altitude and with the autopilot controlling the aircraft, an attempt was made to extend 2º of trailing edge flaps independently of the leading edge slats, probably in an effort to improve aircraft performance<ref name="AAR-81-08 Final Report" />{{rp|32}}}} |
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When retraction of the flaps was ordered, the Number 7 leading edge slat failed to retract, causing the uncommanded roll to the right. |
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{{Blockquote|text=The Safety Board determines that the probable cause of this accident was the isolation of the No. 7 leading edge slat in the fully or partially extended position after an extension of the Nos. 2, 3, 6 and 7 leading edge slats and the subsequent retraction of the Nos. 2, 3, and 6 slats, and the captain's untimely flight control inputs to counter the roll resulting from the slat asymmetry. Contributing to the cause was a preexisting misalignment of the No. 7 slat which, when combined with the cruise condition airloads, precluded retraction of that slat. After eliminating all probable individual or combined mechanical failures, or malfunctions which could lead to slat extension, the Safety Board determined that the extension of the slats was the result of the flightcrew's manipulation of the flap/slat controls. Contributing to the captain's untimely use of the flight controls was distraction due probably to his efforts to rectify the source of the control problem.<ref name="AAR-81-08 Final Report" />{{rp|1}}}} |
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Gibson appealed against the NTSB's findings, first to the NTSB itself and then to the [[U.S. Ninth Circuit Court of Appeals]].<ref name="Tribune 1990.10.14"/><ref>{{cite web|url=https://caselaw.findlaw.com/us-9th-circuit/1188440.html|title=FindLaw's United States Ninth Circuit case and opinions.|publisher=|accessdate=February 6, 2017}}</ref> Both petitions were rejected: the former for lack of new evidence, and the latter for lack of jurisdiction due to the NTSB's "unreviewable discretion". |
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Gibson and the [[Air Line Pilots Association, International|Air Line Pilots Association]] (ALPA) appealed against the NTSB's findings, first to the NTSB itself in 1983, 1990, 1991, 1992, and 1995 and then to the [[U.S. Ninth Circuit Court of Appeals]].<ref name="Tribune 1990.10.14"/><ref>{{cite web|url=https://caselaw.findlaw.com/us-9th-circuit/1188440.html|title=FindLaw's United States Ninth Circuit case and opinions.|publisher=|accessdate=February 6, 2017}}</ref> Both petitions were rejected: the former for lack of new evidence, and the latter for lack of jurisdiction due to the NTSB's "unreviewable discretion".{{Cn|date=September 2024}} |
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The aircraft was repaired and returned to service in May 1979. |
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==Cockpit voice recorder== |
==Cockpit voice recorder== |
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The aircraft was equipped with a Fairchild Industries Model A-100 [[Flight recorder#Cockpit voice recorder|cockpit voice recorder]] (CVR). However, 21 minutes of the 30-minute tape were blank. Tests of the CVR in the aircraft revealed no discrepancies in the CVR's electrical and recording systems.<ref name="AAR-81-08 Final Report" />{{rp|6}} The CVR tape can be erased by means of the bulk-erase feature on the CVR control panel in the cockpit. This feature can be activated only after the aircraft is on the ground with the engines turned off and its parking brake engaged.<ref name="AAR-81-08 Final Report" />{{rp|6}} In a deposition taken by the Safety Board, the captain stated that he usually activates the bulk-erase feature on the CVR at the conclusion of each flight to preclude inappropriate use of recorded conversations. However, in this instance, he and the other two pilots did not recall having done so.<ref name="AAR-81-08 Final Report" />{{rp|6}} Pilot and author Emilio Corsetti III suggested in his book ''Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption,'' that the wiring to the CVR could have been damaged by the heavy, 6 G-force pull out.<ref name="Emilio" />{{rp|page=380}} |
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The aircraft was equipped with a Fairchild Industries Model A-100 [[Flight recorder#Cockpit voice recorder|cockpit voice recorder]] (CVR). However, 21 minutes of the 30-minute tape were blank.<ref name="AAR-81-08 Final Report" />{{rp|6}} Tests of the CVR in the aircraft revealed no discrepancies in the CVR's electrical and recording systems (the NTSB was erroneously told by someone at TWA that there were no faults with the CVR when no tests were ever carried out).<ref name="AAR-81-08 Final Report" />{{rp|6}}The CVR tape can be erased by means of the bulk-erase feature on the CVR control panel located in the cockpit. This feature can be activated only after the aircraft is on the ground with its parking brake engaged.<ref name="AAR-81-08 Final Report" />{{rp|6}} In 1979 it was essentially a standard procedure at the end of every flight to erase the CVR if the flight was routine for privacy reasons <ref>https://emiliocorsetti.com/a-little-background-on-the-cvr/</ref>. In a deposition taken by the Safety Board, the captain stated that he usually activates the bulk-erase feature on the CVR at the conclusion of each flight to preclude inappropriate use of recorded conversations. However, in this instance, he could not recall having done so.<ref name="AAR-81-08 Final Report" />{{rp|6}} The NTSB made the following statement in the accident report: |
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{{Blockquote|We believe the captain's erasure of the CVR is a factor we cannot ignore and cannot sanction. Although we recognize that habits can cause actions not desired or intended by the actor, we have difficulty accepting the fact that the captain's putative habit of routinely erasing the CVR after each flight was not restrainable after a flight in which disaster was only narrowly averted. Our skepticism persists even though the CVR would not have contained any contemporaneous information about the events that immediately preceded the loss of control because we believe it probable that the 25 minutes or more of recording which preceded the landing at Detroit could have provided clues about causal factors and might have served to refresh the flightcrew's memories about the whole matter.<ref name="AAR-81-08 Final Report" />{{rp|33}}}} |
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==Criticism of investigation== |
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In the book ''Emergency: Crisis In the Cockpit'',<ref>{{cite book |title= Emergency! Crisis In The Cockpit |date= January 1, 1991 |isbn= 978-0830634996 |first1= Stanley |last1= Stewart}}</ref> Stanley Stewart, a professional pilot, raised questions about the NTSB findings: |
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*Stewart suggests that the crew would not have been able to erase the CVR as the aircraft had to be completely shut down and on the ground. According to Stewart, the damage should have meant that the computers did not recognize the aircraft in a fully landed state (page 217). |
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*He suggests that there were other incidents of 727-200s with uncommanded slat extensions in the years prior to and after the accident (page 224). |
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*The flight crew knew the aircraft was potentially unstable at 39,000 ft. Stewart believes it would be unlikely they would "fool around" with the controls and risk the stability of the aircraft (page 221). |
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{| class="wikitable" |
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| colspan="3" |'''Excerpt of the CVR transcript; full transcript available in Appendix D.'''<ref name="AAR-81-08 Final Report" />{{rp|40-48}} |
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|- |
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!Source |
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!Content |
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|- |
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|Captain |
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|(Well the) nose gear door |
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|- |
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|Fire Department |
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|Hello Cockpit |
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|- |
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|Radio |
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|Yeah. |
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|- |
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|Fire Department |
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|Ah, did you call operations and request a bus? |
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|- |
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|Radio |
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|No, but we will. |
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|- |
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|Fire Department |
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|Okay, thank you. |
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|- |
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|Unknown |
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|What's the ramp frequency here? |
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|- |
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|Flight Engineer |
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|Detroit one twenty nine one. |
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|- |
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|Unknown |
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|I wonder if there's anybody in there? |
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|- |
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|Unknown |
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|Ah, I hope so. |
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|- |
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|Radio |
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|Ah ramp TWA, this is eight forty one. |
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|- |
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|TWA Ramp |
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|Yeah go ahead. |
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|- |
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|Radio |
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|Ah we've been asked to deplane the passengers, ah, because of a slight fuel leak here. The fire department has asked us to get 'em off and ah we'd like some kind of transportation, a bus for them, please. |
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|- |
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|Radio |
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|What we're going to do is drop the aft stairs and let them walk off ah without excitement, we just want to get them off easily, but we need to get them out of off the taxiway here. |
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|- |
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|TWA Ramp |
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|Yeah, are you still, you still on the runway or? |
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|- |
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|Radio |
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|No, we're on a turnoff from the runway, we're clear of the runway. |
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|- |
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|TWA Ramp |
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|Okay, we'll see what we can do here, is there any way that you can keep in contact with us here? |
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|- |
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|Unknown |
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|Want help? |
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|- |
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|Unknown |
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|Well we won't need that anymore. |
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|- |
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|Unknown |
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|(Looks like) a hydraulic fluid loss huh. |
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|- |
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|Unknown |
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|That's what we were told hydraulic |
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|- |
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|Unknown |
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|Did you feel kind helpless in that seat back there? |
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|- |
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|Unknown |
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|Well, I'll tell you (Believe me). |
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|- |
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|Unknown |
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|You know it's funny to be back here trying to analyze -- this situation. If it happened here, hard to see what's happening, you guys were trying to pull it up. |
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|- |
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|Unknown |
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|Yeah |
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|- |
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|Unknown |
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|Saying get it up, pull it up. like |
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|- |
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|Unknown |
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|That's ah --- emergency descent, as a flyer who wasn't flying it. |
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|- |
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|TWA Ramp |
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|Eight forty one from Detroit ramp. |
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|- |
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|Radio |
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|TWA's eight forty one, go ahead. |
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|- |
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|TWA Ramp |
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|Yes sir, looks like your pretty close to Eastern's terminal there, you think its conceivable that we can walk the people over there, I'm gonna have a hard time gettin' a bus. |
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|- |
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|Radio |
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|Okay, if you could bring somebody over as a guide, I think that would be fine, they wouldn't mind walking that far. |
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|- |
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|Flight Engineer |
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|Okay, what they intend to do Is they cannot get a bus so they're going to bring a guide out and walk them to the Eastern terminal. Ah, whichever one of these it is but in any case they're going to walk them. |
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|- |
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|First Officer |
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|Hoot. |
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|- |
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|Captain |
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|Yeah. |
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|- |
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|Unknown |
|||
|for all the help the people did great, they did exactly what they were told to do. |
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|- |
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|Flight Engineer |
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|That's because you guys took over and did it. |
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|- |
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|Radio |
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|Ah, ramp TWA's eight forty one. Do you need a, any further contact here, if not I'll turn the radios off? |
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|- |
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|TWA Ramp |
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|Ah, no except, ah, can you give me anything, any indication on the airplane or anything dispatch, planning and everybody else is |
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calling, ah can, is there any information that you can give me? |
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|- |
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|Radio |
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|No sir, we can't. I'm sitting in the cockpit and I can't tell you, I don't know what the situation is, you'll have to talk to maintenance. |
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|- |
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|TWA Ramp |
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|Yeah well I mean ah, you lost hydraulic is that it? |
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|- |
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|Radio |
|||
|We assume that's what happened but we can't tell you that what I say until (you) talk to maintenance. |
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|- |
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|TWA Ramp |
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|Okay, you can sign off then. |
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|- |
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|Radio |
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|Detroit Ramp do you read? |
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|- |
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|Radio |
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|Detroit Ramp do you read? |
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|- |
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|'''End Of Recording''' |
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| |
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|} |
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The NTSB made the following statement in the accident report while also acknowledging that the upset and the events leading up to it would not have been recorded:<ref name="AAR-81-08 Final Report" />{{rp|33}} |
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Trans World Airlines and [[Air_Line_Pilots_Association,_International|Air Line Pilots Association]] (ALPA) investigators contend that once the NTSB investigators discovered that 21 minutes of the Cockpit Voice Recorder were blank, instead inspecting it for any deficiencies or ever considering the possibility that it wasn't working properly they quickly concluded the pilots had erased it and developed their own preconceived notion that the pilots had caused the upset instead of letting the evidence lead them to a conclusion. They conducted the investigation with the flight crew's sworn testimonies discounted and elected not to further question them about the events leading up to the upset. The NTSB's conclusions were based on what their biased opinion on what they believed had happened, even though it bore no resemblance to the flight crew or passengers' version of events. <ref>https://emiliocorsetti.com/the-story-of-the-cvr-and-the-man-with-blinders/</ref> |
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{{Blockquote|We believe the captain's erasure of the CVR is a factor we cannot ignore and cannot sanction. Although we recognize that habits can cause actions not desired or intended by the actor, we have difficulty accepting the fact that the captain's putative habit of routinely erasing the CVR after each flight was not restrainable after a flight in which disaster was only narrowly averted. Our skepticism persists even though the CVR would not have contained any contemporaneous information about the events that immediately preceded the loss of control because we believe it probable that the 25 minutes or more of recording which preceded the landing at Detroit could have provided clues about causal factors and might have served to refresh the flightcrew's memories about the whole matter.}} |
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==Criticism of the investigation== |
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=== Air Line Pilots Association (ALPA) === |
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{{Technical|section|date=November 2024}} |
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In ALPA's 1990 petition to the NTSB to reconsider their findings, an analysis conducted by ALPA concluded that the No. 7 slat did not cause the upset and instead extended as a result of the upset. Had the slat caused the upset then it would have detached from the wing at an altitude of around 31,500 feet, not at 8,000 feet.<ref name="Petition for Reconsideration" />{{rp|29}} ALPA concluded that evidence best supported that while cruising at 39,000 feet, the bolt to the outboard right aileron on TWA flight 841 fractured, causing the aileron to [[Aeroelasticity#Flutter|flutter]] and create the high frequency vibration that Captain Gibson reported. As the aileron floated up, the plane banked to the right and turned off its heading, the autopilot tried to correct for this by moving the control wheel left. Once the control wheel turned more than 10°, the spoilers on the left wing deployed to aid in roll control, creating the buzzing sound. With the plane turning right and the autopilot commanding a left turn, the 727 was in a cross-controlled position. The yaw damper rate gyro and or coupler sensed discrepant rudder inputs which resulted in the lower rudder going into the hardover position, causing the plane to yaw severely right. In this condition the left wing produced more lift as a result. A large sideslip angle on sweptback planes like the 727 produces a large rolling moment. |
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Although Gibson disconnected the autopilot and applied opposite aileron and upper rudder, with the lower rudder in the hardover position and limited roll control due to the right outboard aileron free-floating, his control inputs were insufficient to prevent TWA 841 from going into an uncontrollable spiral dive. When the crew lowered the landing gear, the over extension of the right main landing gear ruptured System A hydraulics which centered the lower rudder and allowed the pilots to recover from the dive. Analysis of the No. 7 slat by the NTSB showed a lack of wear, it was misaligned, and didn't lock into its locking mechanism, meaning that it was held in place only by hydraulic pressure and aerodynamic forces. With the loss of hydraulics, the slat extended at 8,000 feet and quickly ripped off. The other slats stayed retracted because they locked into their locking mechanisms.<ref name="Petition for Reconsideration">{{cite web |author1=[[Air Line Pilots Association|Air Line Pilots Association (ALPA)]] |title=Petition for Reconsideration of Probable Cause |url=http://www.iprr.org//comps/pet727/B727_7840.html |website=iprr.org |publisher=Investigation Process Research Resources (IPRR) |access-date=March 8, 2023 |archive-url=https://web.archive.org/web/20071029090350/http://www.iprr.org//comps/pet727/B727_7840.html |archive-date=October 29, 2007 |language=English |date=September 4, 1990}}</ref>{{Verify source|date=September 2024}} |
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=== Stanley Stewart === |
|||
In his book ''Emergency: Crisis In the Cockpit'',<ref name=Emergency!>{{cite book |title= Emergency! Crisis In The Cockpit |date= January 1, 1991 |isbn= 978-0830634996 |first1= Stanley |last1= Stewart|publisher= TAB Books }}</ref> Stanley Stewart, a pilot, asserted the following about the NTSB's findings: |
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*The NTSB conducted 118 tests in a flight simulator with the isolated extension of the No. 7 slat and the aircraft was easily controllable in that condition. According to Steward, there was no correlation between the simulator traces of these maneuvers and Flight 841's FDR traces.<ref name="AAR-81-08 Final Report" />{{rp|9}}<ref name=Emergency!/>{{rp|page=209}} |
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*Although it was not determined when the outboard aileron bolt fractured, if it did fracture before the upset, it would have permitted free-play which would induce a right roll thereby contributing to the upset.<ref name=Emergency!/>{{rp|page=212}} The simulator tests did not take into consideration free-play of the right outboard aileron.<ref name="AAR-81-08 Final Report" />{{rp|9}} |
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*The extension of the slats would cause more than a moderate buffeting of the airframe while Captain Gibson reported only a light buffeting.<ref name=Emergency!/>{{rp|page=214}} <ref name="AAR-81-08 Final Report" />{{rp|2, 13}} |
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*The crew would not have been able to erase the CVR as the aircraft had to be completely shut down and on the ground. According to Stewart the damage would have meant that the computers did not recognize the aircraft in a fully landed state.<ref name=Emergency!/>{{rp|page=217}} |
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*A CVR technical expert interviewed for [[Popular Mechanics]] contended that the slow transfer of electrical power from engine power to the APU after it was turned on likely caused the erasure of the CVR.<ref name=Emergency!/>{{rp|page=217}} |
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*The pilots, along with the flight attendants and 14 passengers including four or five first class passengers, stated that Second Officer Banks had not left the cockpit just before the upset. Instead, Captain Gibson maintained that Banks had only briefly left the cockpit 30 minutes prior to the upset.<ref name=Emergency!/>{{rp|page=218}} |
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*Stewart found it rather absurd that Second Officer Banks, supposedly returning to the cockpit right before the upset, would notice the pulled circuit breaker behind crew coats in a dark cockpit and pushed it back in without saying anything to the other pilots. And if the practice of extending the flaps to the 2° was widespread then he would not have pushed the breaker back in. Stewart stated: "The NTSB scenario did not fit the facts and, even if the crew had deliberately set 2° of flap as entertained here, the extension of the number seven leading edge slat was highly unlikely to have happened in this manner".<ref name=Emergency!/>{{rp|page=218}} |
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*The NTSB investigators questioned passengers seated over the wings if they heard any unusual sounds before the upset, such as the high pitched shrill of the hydraulic flap motors as the pilots, supposedly, extended them and then later retracted to rectify the extension of the slats to which they said no. According to Stewart, this alone suggested that the flaps were not extended in cruise flight.<ref name=Emergency!/>{{rp|page=221}} |
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*Stewart claimed that the entire investigation was conducted with the flight crew absent except for shortly after they landed and two public hearings. After these hearings, during the intervals between the two and the release of the Final Report, the flight crew were never consulted, cross examined, or questioned by any investigator, and all of the Captain's phone calls to the NTSB were refused.<ref name=Emergency!/>{{rp|page=222}} |
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*Stewart contended that the flight crew knew the aircraft was potentially unstable at 39,000 ft. Stewart believed it would be unlikely that they would "fool around" with the controls and risk the stability of the aircraft.<ref name=Emergency!/>{{rp|page=221}} |
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*He stated that there were other incidents of 727-200s with uncommanded slat extensions in the years prior to and after the accident.<ref name=Emergency!/>{{rp|page=224}} |
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=== Emilio Corsetti III === |
|||
Professional pilot and author, Emilio Corsetti III, stated in his book ''Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption'', <ref>{{cite book |title= Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption |date= August 1, 2016 |isbn= 978-80997242102 |first1= Emilio |last1 Corsetti III}}</ref> that the Boeing engineers and NTSB investigators massaged the data to make it match their version of events, not the flight crew's version of events (page 192); and "had the NTSB not let the supposed erasure of the CVR implant a bias on the investigation, they might have considered possibilities other than crew involvement. They might have talked to the crew in greater detail and would have learned that the plane yawed before the upset" (page 384). |
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Emilio Corsetti III stated in his book, ''Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption'',<ref name="Emilio">{{cite book |title= Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption |date= August 1, 2016 |isbn= 978-0997242102 |first1= Emilio |last1= Corsetti III|publisher= Odyssey Publishing, LLC }}</ref> that the Boeing engineers and NTSB investigators had massaged the data to make it match what they thought happened, not the flight crew's version of events;<ref name="Emilio" />{{rp|page=192}} and stated that "had the NTSB not let the supposed erasure of the CVR implant a bias on the investigation, they might have considered possibilities other than crew involvement. They might have talked to the crew in greater detail and would have learned that the plane yawed before the upset".<ref name="Emilio" />{{rp|page=384}} |
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==In media== |
==In media== |
||
This |
This accident was the subject of a [[CBS|CBS News]] Special titled, "The Plane That Fell From the Sky". The special won a [[Peabody Award]] in [[List of Peabody Award winners (1980–89)#1983|1983]].<ref>{{cite web|url=http://www.peabodyawards.com/award-profile/the-plane-that-fell-from-the-sky|title=The Plane That Fell From the Sky|publisher=|accessdate=February 6, 2017}}</ref> |
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The |
The accident was featured on season 22 of the Canadian documentary series ''[[Mayday (Canadian TV series)|Mayday]]'', in the episode titled "Terror over Michigan".<ref>{{cite web |title=Terror over Michigan |author= Air Crash Investigation |url=https://www.imdb.com/title/tt15799988/?ref_=tt_ep_nx |website=IMDb}}</ref> |
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==See also== |
==See also== |
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* [[China Airlines Flight 006]] - Another case where a [[Boeing]] aircraft entered an uncontrolled nose-dive |
* [[China Airlines Flight 006]] - Another case where a [[Boeing]] aircraft entered an uncontrolled nose-dive |
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* [[China Eastern Airlines Flight 583]] — Another slat extension in-flight accident |
* [[China Eastern Airlines Flight 583]] — Another slat extension in-flight accident |
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* [[Partnair Flight 394]] - Another instance where using the APU as the power source caused a stoppage in recording of the Cockpit Voice Recorder. |
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* [[United Airlines Flight 585]] |
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* [[USAir Flight 427]] |
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* [[Eastwind Flight 517]] |
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==References== |
==References== |
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==External links== |
==External links== |
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*{{ASN accident|id=19790404-0}} |
*{{ASN accident|id=19790404-0}} |
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*[https://www.ntsb.gov/ |
*[https://www.ntsb.gov/investigations/Pages/DCA79AA016.aspx NTSB Investigation] |
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*[http://caselaw.lp.findlaw.com/cgi-bin/getcase.pl?court=9th&navby=case&no=9570525 U.S. Ninth Circuit Court of Appeals, GIBSON v NTSB (appeal dismissed--lack of jurisdiction)] |
*[http://caselaw.lp.findlaw.com/cgi-bin/getcase.pl?court=9th&navby=case&no=9570525 U.S. Ninth Circuit Court of Appeals, GIBSON v NTSB (appeal dismissed--lack of jurisdiction)] |
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{{Aviation accidents and incidents in 1979}} |
{{Aviation accidents and incidents in 1979}} |
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{{Aviation accidents and incidents in the United States in the 1970s}} |
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{{TWA}} |
{{TWA}} |
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[[Category:Accidents and incidents involving the Boeing 727]] |
[[Category:Accidents and incidents involving the Boeing 727]] |
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[[Category:Airliner accidents and incidents in Michigan]] |
[[Category:Airliner accidents and incidents in Michigan]] |
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[[Category:Disasters in Michigan]] |
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[[Category:1979 in Michigan]] |
[[Category:1979 in Michigan]] |
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[[Category:April 1979 events in the United States]] |
[[Category:April 1979 events in the United States]] |
Latest revision as of 21:14, 3 January 2025
Accident | |
---|---|
Date | April 4, 1979 |
Summary | Uncontrolled descent; cause disputed |
Site | Over Saginaw, Michigan, United States |
Aircraft | |
Aircraft type | Boeing 727-31 |
Operator | Trans World Airlines |
IATA flight No. | TW841 |
ICAO flight No. | TWA841 |
Call sign | TWA 841 |
Registration | N840TW |
Flight origin | John F. Kennedy International Airport, New York City, U.S. |
Destination | Minneapolis-Saint Paul International Airport, Minneapolis, U.S. |
Occupants | 89 |
Passengers | 82 |
Crew | 7 |
Fatalities | 0 |
Injuries | 8 |
Survivors | 89 |
TWA Flight 841 was a scheduled passenger flight from John F. Kennedy International Airport, New York City, en route to Minneapolis-Saint Paul International Airport in Minneapolis, Minnesota. On the evening of April 4, 1979 while flying over Saginaw, Michigan, the Boeing 727-31 airliner began a sharp, uncommanded roll to the right, and subsequently went into a spiral dive. The pilots were able to regain control of the aircraft and made an emergency landing at Detroit Metropolitan Airport.
Background
[edit]Aircraft
[edit]The aircraft involved, manufactured in 1965, was a 13 year old Boeing 727-31, registered as N840TW with serial number 18905. In its 14 years of service, it had accumulated about 35,412 hours.[1]: 8
Crew
[edit]In command was Captain Harvey G. "Hoot" Gibson, aged 44, who had logged a total of 15,710 piloting hours, 2,597 of them on the 727. The day before he had returned to flying following a three month medical leave.[1]: 4 The First Officer was J. Scott Kennedy, aged 40, who had logged a total of 10,336 total piloting hours, 8,348 of them on the 727. The flight engineer was Gary N. Banks, 37, who had logged a total of 4,186 piloting hours, 1,186 of them on the 727.[1]: 8
Accident
[edit]At 8:25 p.m. EST, TWA Flight 841 departed JFK International after a 45-minute delay due to traffic congestion and reached its initial cruising altitude of 35,000 feet at 8:54 p.m. Due to a 100-knot headwind, the pilots requested to climb to 39,000 feet at 9:25 p.m., which was granted. At 9:47 p.m., while cruising at 39,000 feet (12,000 m) near the city of Saginaw, Michigan, Captain Gibson said the aircraft was operating with the autopilot on "Altitude Hold" mode when he felt a high frequency vibration in the balls of his feet, followed by a buzzing sound and a light buffeting of the airframe. He looked at his instruments and saw the plane banking right before yawing sharply to the right, briefly pausing, and yawing right again into a skidding right roll with the autopilot moving the control wheel to the left to level the wings.[2]: 194-195 Gibson disconnected the autopilot and applied full left aileron which had no effect. He got on the rudder pedals and applied full left rudder. As he did so something didn't feel right but he couldn't place it.[3]: 11 Although Captain Gibson's inputs briefly stopped the roll from increasing, the roll continued and the aircraft spiraled out of control. Gibson shouted something to the effect of "We're going over!"[1]: 6 After completing one 360° roll, Gibson shouted to the co-pilot "Get em' up!" referring him to deploy the speed brakes, but the co-pilot didn't understand what the Captain meant so Gibson deployed them which also had no effect.[1]: 2–3
Flight 841 dove about 34,000 feet (10,000 m) in just 63 seconds.[1]: 2 During the course of the dive, the plane rolled through 360 degrees at least twice and exceeded the Mach limit for the 727 airframe.
At about 15,000 feet (4,600 m) the pilots extended the landing gear in an attempt to slow the aircraft. A few seconds after extending the gear, Gibson managed to regain control and pulled the 727 out of its dive at about 5,000 feet (1,500 m).[4][5] The plane suffered substantial structural damage with the No.7 leading-edge slat and a flight spoiler having detached, the right outboard aileron hinge fitting broke due to metal fatigue resulting in free-play, and the System A hydraulics ruptured due to the right main gear overextending which also broke the sidebrace and actuator support beam; the Flight Engineer reported they had a fail flag for the lower rudder yaw damper[1]: 10 but made an emergency landing at Detroit Metropolitan Airport in Michigan at 10:31 p.m. EST without further trouble. After landing and shutting the engines down the pilots turned on the Auxiliary Power Unit (APU) as a mechanic plugged into an intercom to talk to the pilots and reported fuel was leaking from the left side. All 89 people deplaned via the aft airstair with only eight passengers suffering minor injuries.[1]
Investigation
[edit]Several days after the upset, the aircraft was sufficiently repaired to be ferried to Kansas City for further repairs instead of being preserved for tests and in-depth analysis of components and systems in order to conclusively determine what happened; it returned to service in May 1979.[1]: 4 The flight crew would be questioned on three occasions during the course of the entire investigation: hours after landing in Detroit, on April 12, 1979, and on January 29, 1980.[1]: 37 The investigators of the National Transportation Safety Board (NTSB) located the No. 7 slat missing from the leading edge of the right wing amongst other parts that had detached. They requested that Boeing, the manufacturer, inspect the remainder of the slat assembly, including a portion of the slat actuator cylinder (the motor that moves the slat and holds it in position). Boeing determined that the No. 7 slat had failed because the slats had been extended while the aircraft was flying at cruising speed. They also determined that it was "impossible" for the slat to extend without manipulating the controls.[6][better source needed]
The TWA Flight 841 investigation would be at the time the lengthiest accident investigation in the NTSB's history.[7] After eliminating all known sources of mechanical failure, the NTSB concluded in June 1981 in its final report, that the probable cause of the accident was the isolated extension of the No. 7 leading-edge slat from the flight crew manipulating the flap/slat controls in an inappropriate manner leading to an uncommanded roll to the right and the captain's untimely action.[8][1]: 1–2
The Safety Board determines that the probable cause of this accident was the isolation of the No. 7 leading-edge slat in the fully or partially extended position after an extension of the Nos. 2, 3, 6 and 7 leading-edge slats and the subsequent retraction of the Nos. 2, 3, and 6 slats, and the captain's untimely flight control inputs to counter the roll resulting from the slat asymmetry. Contributing to the cause was a preexisting misalignment of the No. 7 slat which, when combined with the cruise condition airloads, precluded retraction of that slat. After eliminating all probable individual or combined mechanical failures, or malfunctions which could lead to slat extension, the Safety Board determined that the extension of the slats was the result of the flightcrew's manipulation of the flap/slat controls. Contributing to the captain's untimely use of the flight controls was distraction due probably to his efforts to rectify the source of the control problem.[1]: 1
Investigators believed that 727 pilots (in general, and this crew specifically) were enabling the trailing edge flaps to extend independently of the slats via the flap/slat lever by turning the Alternate flap switch on, pulling the leading-edge slats circuit breaker, turning the Alternate flap switch off and then setting the flaps to two degrees during high altitude cruise. This configuration was rumored to result in increased lift with no increase in drag, thus allowing more speed, higher elevation, or decreased fuel consumption. Flight tests showed that airspeed and performance decreased in this configuration. Flaps and slats are intended to only be deployed at low speeds during take-off and landing.[1]
The crew, Capt. Harvey G. "Hoot" Gibson (1934–2015),[9] First Officer J. Scott Kennedy (1939–2017),[10] and Flight Engineer Gary N. Banks (born 1942), denied that their actions had been the cause of the flaps' extension:
At no time prior to the incident did I take any action within the cockpit either intentionally or inadvertently, that would have caused the extension of the leading edge slats or trailing edge flaps. Nor did I observe any other crew member take any action within the cockpit, either intentional or inadvertent, which would have caused the extension.
The flight crew testified that they had not engaged the flaps and instead suggested that the actuator to the No. 7 slat had failed, causing its inadvertent deployment. The NTSB concluded that "if the flight crew's recollections are accurate," the slat extension must have been caused by a mechanical failure or defect but ultimately rejected this as improbable and attributed the extension of the flaps to the deliberate actions of the crew.[1]: 24 The crew maintained that such failures had happened on other 727s prior and subsequent to this incident.[13] The NTSB report noted seven separate cases involving a single leading edge slat extension and separation were reported between 1970 and 1973, but none of these reports indicated whether or not the slat extension was due to flight crew involvement.[1]: 18 Records after 1974 did include two report slat extensions between 1974 and towards the end of the NTSB's investigation in 1981, one of which was inadvertently caused by the flight crew. However, in none of these previous cases did the flights experience significant problems.[1]: 24
Gibson and the Air Line Pilots Association (ALPA) appealed against the NTSB's findings, first to the NTSB itself in 1983, 1990, 1991, 1992, and 1995 and then to the U.S. Ninth Circuit Court of Appeals.[7][14] Both petitions were rejected: the former for lack of new evidence, and the latter for lack of jurisdiction due to the NTSB's "unreviewable discretion".[citation needed]
Cockpit voice recorder
[edit]The aircraft was equipped with a Fairchild Industries Model A-100 cockpit voice recorder (CVR). However, 21 minutes of the 30-minute tape were blank. Tests of the CVR in the aircraft revealed no discrepancies in the CVR's electrical and recording systems.[1]: 6 The CVR tape can be erased by means of the bulk-erase feature on the CVR control panel in the cockpit. This feature can be activated only after the aircraft is on the ground with the engines turned off and its parking brake engaged.[1]: 6 In a deposition taken by the Safety Board, the captain stated that he usually activates the bulk-erase feature on the CVR at the conclusion of each flight to preclude inappropriate use of recorded conversations. However, in this instance, he and the other two pilots did not recall having done so.[1]: 6 Pilot and author Emilio Corsetti III suggested in his book Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption, that the wiring to the CVR could have been damaged by the heavy, 6 G-force pull out.[3]: 380
Excerpt of the CVR transcript; full transcript available in Appendix D.[1]: 40–48 | ||
Source | Content | |
---|---|---|
Captain | (Well the) nose gear door | |
Fire Department | Hello Cockpit | |
Radio | Yeah. | |
Fire Department | Ah, did you call operations and request a bus? | |
Radio | No, but we will. | |
Fire Department | Okay, thank you. | |
Unknown | What's the ramp frequency here? | |
Flight Engineer | Detroit one twenty nine one. | |
Unknown | I wonder if there's anybody in there? | |
Unknown | Ah, I hope so. | |
Radio | Ah ramp TWA, this is eight forty one. | |
TWA Ramp | Yeah go ahead. | |
Radio | Ah we've been asked to deplane the passengers, ah, because of a slight fuel leak here. The fire department has asked us to get 'em off and ah we'd like some kind of transportation, a bus for them, please. | |
Radio | What we're going to do is drop the aft stairs and let them walk off ah without excitement, we just want to get them off easily, but we need to get them out of off the taxiway here. | |
TWA Ramp | Yeah, are you still, you still on the runway or? | |
Radio | No, we're on a turnoff from the runway, we're clear of the runway. | |
TWA Ramp | Okay, we'll see what we can do here, is there any way that you can keep in contact with us here? | |
Unknown | Want help? | |
Unknown | Well we won't need that anymore. | |
Unknown | (Looks like) a hydraulic fluid loss huh. | |
Unknown | That's what we were told hydraulic | |
Unknown | Did you feel kind helpless in that seat back there? | |
Unknown | Well, I'll tell you (Believe me). | |
Unknown | You know it's funny to be back here trying to analyze -- this situation. If it happened here, hard to see what's happening, you guys were trying to pull it up. | |
Unknown | Yeah | |
Unknown | Saying get it up, pull it up. like | |
Unknown | That's ah --- emergency descent, as a flyer who wasn't flying it. | |
TWA Ramp | Eight forty one from Detroit ramp. | |
Radio | TWA's eight forty one, go ahead. | |
TWA Ramp | Yes sir, looks like your pretty close to Eastern's terminal there, you think its conceivable that we can walk the people over there, I'm gonna have a hard time gettin' a bus. | |
Radio | Okay, if you could bring somebody over as a guide, I think that would be fine, they wouldn't mind walking that far. | |
Flight Engineer | Okay, what they intend to do Is they cannot get a bus so they're going to bring a guide out and walk them to the Eastern terminal. Ah, whichever one of these it is but in any case they're going to walk them. | |
First Officer | Hoot. | |
Captain | Yeah. | |
Unknown | for all the help the people did great, they did exactly what they were told to do. | |
Flight Engineer | That's because you guys took over and did it. | |
Radio | Ah, ramp TWA's eight forty one. Do you need a, any further contact here, if not I'll turn the radios off? | |
TWA Ramp | Ah, no except, ah, can you give me anything, any indication on the airplane or anything dispatch, planning and everybody else is
calling, ah can, is there any information that you can give me? | |
Radio | No sir, we can't. I'm sitting in the cockpit and I can't tell you, I don't know what the situation is, you'll have to talk to maintenance. | |
TWA Ramp | Yeah well I mean ah, you lost hydraulic is that it? | |
Radio | We assume that's what happened but we can't tell you that what I say until (you) talk to maintenance. | |
TWA Ramp | Okay, you can sign off then. | |
Radio | Detroit Ramp do you read? | |
Radio | Detroit Ramp do you read? | |
End Of Recording |
The NTSB made the following statement in the accident report while also acknowledging that the upset and the events leading up to it would not have been recorded:[1]: 33
We believe the captain's erasure of the CVR is a factor we cannot ignore and cannot sanction. Although we recognize that habits can cause actions not desired or intended by the actor, we have difficulty accepting the fact that the captain's putative habit of routinely erasing the CVR after each flight was not restrainable after a flight in which disaster was only narrowly averted. Our skepticism persists even though the CVR would not have contained any contemporaneous information about the events that immediately preceded the loss of control because we believe it probable that the 25 minutes or more of recording which preceded the landing at Detroit could have provided clues about causal factors and might have served to refresh the flightcrew's memories about the whole matter.
Criticism of the investigation
[edit]Air Line Pilots Association (ALPA)
[edit]This section may be too technical for most readers to understand.(November 2024) |
In ALPA's 1990 petition to the NTSB to reconsider their findings, an analysis conducted by ALPA concluded that the No. 7 slat did not cause the upset and instead extended as a result of the upset. Had the slat caused the upset then it would have detached from the wing at an altitude of around 31,500 feet, not at 8,000 feet.[15]: 29 ALPA concluded that evidence best supported that while cruising at 39,000 feet, the bolt to the outboard right aileron on TWA flight 841 fractured, causing the aileron to flutter and create the high frequency vibration that Captain Gibson reported. As the aileron floated up, the plane banked to the right and turned off its heading, the autopilot tried to correct for this by moving the control wheel left. Once the control wheel turned more than 10°, the spoilers on the left wing deployed to aid in roll control, creating the buzzing sound. With the plane turning right and the autopilot commanding a left turn, the 727 was in a cross-controlled position. The yaw damper rate gyro and or coupler sensed discrepant rudder inputs which resulted in the lower rudder going into the hardover position, causing the plane to yaw severely right. In this condition the left wing produced more lift as a result. A large sideslip angle on sweptback planes like the 727 produces a large rolling moment.
Although Gibson disconnected the autopilot and applied opposite aileron and upper rudder, with the lower rudder in the hardover position and limited roll control due to the right outboard aileron free-floating, his control inputs were insufficient to prevent TWA 841 from going into an uncontrollable spiral dive. When the crew lowered the landing gear, the over extension of the right main landing gear ruptured System A hydraulics which centered the lower rudder and allowed the pilots to recover from the dive. Analysis of the No. 7 slat by the NTSB showed a lack of wear, it was misaligned, and didn't lock into its locking mechanism, meaning that it was held in place only by hydraulic pressure and aerodynamic forces. With the loss of hydraulics, the slat extended at 8,000 feet and quickly ripped off. The other slats stayed retracted because they locked into their locking mechanisms.[15][verification needed]
Stanley Stewart
[edit]In his book Emergency: Crisis In the Cockpit,[2] Stanley Stewart, a pilot, asserted the following about the NTSB's findings:
- The NTSB conducted 118 tests in a flight simulator with the isolated extension of the No. 7 slat and the aircraft was easily controllable in that condition. According to Steward, there was no correlation between the simulator traces of these maneuvers and Flight 841's FDR traces.[1]: 9 [2]: 209
- Although it was not determined when the outboard aileron bolt fractured, if it did fracture before the upset, it would have permitted free-play which would induce a right roll thereby contributing to the upset.[2]: 212 The simulator tests did not take into consideration free-play of the right outboard aileron.[1]: 9
- The extension of the slats would cause more than a moderate buffeting of the airframe while Captain Gibson reported only a light buffeting.[2]: 214 [1]: 2, 13
- The crew would not have been able to erase the CVR as the aircraft had to be completely shut down and on the ground. According to Stewart the damage would have meant that the computers did not recognize the aircraft in a fully landed state.[2]: 217
- A CVR technical expert interviewed for Popular Mechanics contended that the slow transfer of electrical power from engine power to the APU after it was turned on likely caused the erasure of the CVR.[2]: 217
- The pilots, along with the flight attendants and 14 passengers including four or five first class passengers, stated that Second Officer Banks had not left the cockpit just before the upset. Instead, Captain Gibson maintained that Banks had only briefly left the cockpit 30 minutes prior to the upset.[2]: 218
- Stewart found it rather absurd that Second Officer Banks, supposedly returning to the cockpit right before the upset, would notice the pulled circuit breaker behind crew coats in a dark cockpit and pushed it back in without saying anything to the other pilots. And if the practice of extending the flaps to the 2° was widespread then he would not have pushed the breaker back in. Stewart stated: "The NTSB scenario did not fit the facts and, even if the crew had deliberately set 2° of flap as entertained here, the extension of the number seven leading edge slat was highly unlikely to have happened in this manner".[2]: 218
- The NTSB investigators questioned passengers seated over the wings if they heard any unusual sounds before the upset, such as the high pitched shrill of the hydraulic flap motors as the pilots, supposedly, extended them and then later retracted to rectify the extension of the slats to which they said no. According to Stewart, this alone suggested that the flaps were not extended in cruise flight.[2]: 221
- Stewart claimed that the entire investigation was conducted with the flight crew absent except for shortly after they landed and two public hearings. After these hearings, during the intervals between the two and the release of the Final Report, the flight crew were never consulted, cross examined, or questioned by any investigator, and all of the Captain's phone calls to the NTSB were refused.[2]: 222
- Stewart contended that the flight crew knew the aircraft was potentially unstable at 39,000 ft. Stewart believed it would be unlikely that they would "fool around" with the controls and risk the stability of the aircraft.[2]: 221
- He stated that there were other incidents of 727-200s with uncommanded slat extensions in the years prior to and after the accident.[2]: 224
Emilio Corsetti III
[edit]Emilio Corsetti III stated in his book, Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption,[3] that the Boeing engineers and NTSB investigators had massaged the data to make it match what they thought happened, not the flight crew's version of events;[3]: 192 and stated that "had the NTSB not let the supposed erasure of the CVR implant a bias on the investigation, they might have considered possibilities other than crew involvement. They might have talked to the crew in greater detail and would have learned that the plane yawed before the upset".[3]: 384
In media
[edit]This accident was the subject of a CBS News Special titled, "The Plane That Fell From the Sky". The special won a Peabody Award in 1983.[16]
The accident was featured on season 22 of the Canadian documentary series Mayday, in the episode titled "Terror over Michigan".[17]
See also
[edit]- China Airlines Flight 006 - Another case where a Boeing aircraft entered an uncontrolled nose-dive
- China Eastern Airlines Flight 583 — Another slat extension in-flight accident
- Partnair Flight 394 - Another instance where using the APU as the power source caused a stoppage in recording of the Cockpit Voice Recorder.
- United Airlines Flight 585
- USAir Flight 427
- Eastwind Flight 517
References
[edit]- ^ a b c d e f g h i j k l m n o p q r s t u v w x Aircraft Accident Report - Trans World Airlines, Inc., Boeing 727-31, N840TW, Near Saginaw, Michigan April 4, 1979 (PDF). National Transportation Safety Board. June 9, 1981. - Copy at Embry-Riddle Aeronautical University.
- ^ a b c d e f g h i j k l m Stewart, Stanley (January 1, 1991). Emergency! Crisis In The Cockpit. TAB Books. ISBN 978-0830634996.
- ^ a b c d e Corsetti III, Emilio (August 1, 2016). Scapegoat: A Flight Crew's Journey From Heroes to Villains to Redemption. Odyssey Publishing, LLC. ISBN 978-0997242102.
- ^ Peterson, Iver. "Plane Passengers Prayed But Expected to Be Killed." The New York Times (April 7, 1979), 6.
- ^ The Post-Standard (Syracuse, New York), June 10, 1981, page 11
- ^ otosflashymoon (September 17, 2012). "The Plane That Fell From The Sky (Full Version) TWA 841". Archived from the original on December 15, 2021. Retrieved February 6, 2017 – via YouTube.
- ^ a b "11 Years After Plane Took A Dive, Pilot Tries To Clear His Reputation". Chicago Tribune. October 14, 1990. Retrieved February 6, 2017.
- ^ Witkin, Richard. "Safety Board Hints Crew Errors May Have Led to Jet Dive Over Michigan." The New York Times (January 18, 1980), A10.
- ^ "Hoot Gibson remembered". February 2015.
- ^ "The passing of Scott Kennedy". October 26, 2017.
- ^ Witkin, Richard. "Crew Will Testify Today On Near-Fatal Jet Plunge." The New York Times (Apr 12, 1979), B10.
- ^ Lindsey, Robert. "Pilot Says Extending Landing Gear Was Near Last Resort to Stop Dive." The New York Times (Apr 13, 1979), A16.
- ^ Boeing Operations Manual Bulletin, OMB 75-7, March 10, 1976; Subject: "Leading Edge Slat Actuator Lock Rings"; outlined specific conditions which had previously resulted in a Leading Edge Slat being pulled from the Retracted position (Mach > .8M, with failure of "A" System Hydraulic pressure to the slat actuator, with SpeedBrakes/Spoilers Extended).
- ^ "FindLaw's United States Ninth Circuit case and opinions". Retrieved February 6, 2017.
- ^ a b Air Line Pilots Association (ALPA) (September 4, 1990). "Petition for Reconsideration of Probable Cause". iprr.org. Investigation Process Research Resources (IPRR). Archived from the original on October 29, 2007. Retrieved March 8, 2023.
- ^ "The Plane That Fell From the Sky". Retrieved February 6, 2017.
- ^ Air Crash Investigation. "Terror over Michigan". IMDb.